xtracrispy
Well-known member
- May 5, 2021
- 228
- 264
Picked up an 85 ATC250r couple months back. Been running 32:1 Super Techniplate or Castor 927 with premium gas. Stock intake and carb, UNI filter, Dg pipe, FMF silencer, Stock bore, Boyeson 2 stage power reeds.
Took it out last trip with no significant issues. Seemed like it was loading up and running real rich while cruising 1/4-1/2 throttle. Poor throttle response, pulled ok in the powerband, seemed like it signed off kinda early. But you couldn't clutch it to keep the power if it fell out of the powerband, once it fell out it was gone, even downshifting and clutching. Smoked a bit, breaking up wile cruising 1/4-1/2 throttle, plug was black and wet. Stock jetting, 52 pilot, 152 main, needle in second clip from top(second from lowest needle position). Dropped the needle all the way with maybe a little improvement.
Second trip(last weekend), rejetted with 48 Pilot, 154 main, needle in middle clip(hoping to lean the bottom for better throttle response with richer mid-top for cooling and hopefully better pull on hills), no other changes(except a twist throttle conversion). First run to Olds from washes: better throttle response, less breaking up. Thought I heard some pinging pulling Olds but seemed to run better overall. Next ride at moderate pace, missed a shift and got stuck on a hill. While turning around smelled coolant, overflow tank was higher than normal, looked at my temp strips and they were high (226F or so). Decided to head back to camp, while cruising back temp strips indicated similar temps, higher than I was used to seeing, blew the upper crossover coolant hose about half way back to camp and had to be towed.
Plug looked good, water pump still spins, not seized.
What should I check next? Pressure test the coolant system? I don't think I'm running lean enough to cause it to get that hot.
Took it out last trip with no significant issues. Seemed like it was loading up and running real rich while cruising 1/4-1/2 throttle. Poor throttle response, pulled ok in the powerband, seemed like it signed off kinda early. But you couldn't clutch it to keep the power if it fell out of the powerband, once it fell out it was gone, even downshifting and clutching. Smoked a bit, breaking up wile cruising 1/4-1/2 throttle, plug was black and wet. Stock jetting, 52 pilot, 152 main, needle in second clip from top(second from lowest needle position). Dropped the needle all the way with maybe a little improvement.
Second trip(last weekend), rejetted with 48 Pilot, 154 main, needle in middle clip(hoping to lean the bottom for better throttle response with richer mid-top for cooling and hopefully better pull on hills), no other changes(except a twist throttle conversion). First run to Olds from washes: better throttle response, less breaking up. Thought I heard some pinging pulling Olds but seemed to run better overall. Next ride at moderate pace, missed a shift and got stuck on a hill. While turning around smelled coolant, overflow tank was higher than normal, looked at my temp strips and they were high (226F or so). Decided to head back to camp, while cruising back temp strips indicated similar temps, higher than I was used to seeing, blew the upper crossover coolant hose about half way back to camp and had to be towed.
Plug looked good, water pump still spins, not seized.
What should I check next? Pressure test the coolant system? I don't think I'm running lean enough to cause it to get that hot.